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SERVICEMAN’S LOG
The show must go on
Dave Thompson
The servicing gods must have some kind of influence in our lives;
otherwise, how would it be that very similar jobs end up in the workshop at
the same time? Kismet? Synchronicity? Pure coincidence? Dumb luck?
It happened that I received two large TVs, a turntable and
a DVD player to repair, all arriving within days of each other.
Now, I have repaired TVs before and found them to be
challenging. In fact, I recall helping out my uncle in Melbourne with simple jobs when he ran a thriving TV hire
and repair business back in the 1980s. I was on holiday
there and loved his workshops, with the mirrors on the
back wall so he could watch what the TV was doing as he
poked and prodded around in the back of it.
I cannot tell a lie, those high-tension leads scared me,
and I remember both Dad and him somehow creating huge
fat arcs of electricity to the end of screwdrivers just for fun!
Not for me, thank you!
Of course, those TVs were very different, being huge,
heavy things with CRTs and large transformers and discrete
circuitry – some even still used valves, which were always
fun to work with, in a shocking sort of way. I’ve built dozens of guitar amplifiers, both solid-state and valve-based,
but they don’t scare me as much as those old things did.
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I have had people ask me if I can look at their old sets –
they are into the retro thing but use set-top boxes of some
sort to get ‘modern’ signals. I just politely decline; I don’t
really know what I’m doing with them, and would likely
end up cooking myself on the flyback transformer output.
The very model of a modern modular monitor
Modern TVs, however, are a different story. Most are
now modular, with several circuit boards inside, all performing their separate functions. That makes any repair a
lot easier, as long as you can get the boards.
The power supply is obvious. It powers any LED backlighting (on older sets) and of course provides power to all
the other boards. There is usually a main board that controls video and audio feeds and sends them to the right
place (amongst other things like storing settings and personal channel choices).
There is also sometimes a T-Con board, short for “timing
controller”, which ensures the signals go to the right place
at the right time. Some TVs don’t have these
T-Con boards as a separate module; it is
all incorporated into the main board.
So, there is lots going on inside modern TV. Of course, OLED TVs are very
similar to LCDs, just with a different
type of screen at the front and suitable
circuitry to drive it. The rest is pretty
much the same.
I ended up with two LED (backlit
LCD) TVs in the workshop. Anyone
who has seen my workshop knows that
it is quite small and that it looks like a
grenade has gone off inside. So having
two rather large TVs in there makes it
difficult to move around, which is why
I usually don’t take on big jobs (both
figuratively and literally).
The first TV is one of several models sold by a local big-box store that
are priced quite reasonably for their
size and specifications. However,
there is often a price to pay when
buying cheap. This one had no video
output, although there was audio, and
the remote control seemed to operate
all the settings, if the volume was anything to go by.
With this type of display, it always
pays to have a good look at it from the
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
• The show must go on
• Fixing two broken laptops
• The danger of high-impedance measurements
• Hickok TV-7 valve tester repair
• Repairing a Seiko wall clock
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
side, especially if you’re in poor light. If you can see shadows moving from that angle, it indicates that the panel is
doing its thing and the fault is with the backlight. However,
in this case, I could see nothing; not good, then.
It could be a power supply failure, a screen failure or
a mainboard failure. Or even a T-Con board failure. That
really narrows it down (not)!
It is difficult to get the parts you need to repair these at a
component level because these things are all modular now.
If something fails, you’re supposed to pull the board, replace
it and off you go. However, new boards can be pricey!
The evils of a throw-away society
I suspect that if these things are returned under warranty,
they just give the customer a new one and throw the old
one in a skip, which is criminal. The amount of e-waste we
generate for such a small country is embarrassing.
I know of a printer repair shop that has a literal mountain
of old printers, most of which could be repaired with a $10
part (if that). However, because these parts are not available, they just get dumped; the pile is cleared twice a year!
Yes, some printer companies have a returns policy where
you can take your old one in and they’ll dispose of it. However, that usually means filling containers with this branded
waste and sending it to somewhere like Malaysia, Indonesia or (less likely these days) China. The people there
either burn it in big piles or smelt it down in crude village
furnaces to get any precious metals out of it.
The problem is that all the toxins from these basic processes leach into the soil and cause all manner of birth
defects and pollution. It certainly makes me think when I
am getting rid of an old printer.
Anyway, back to the TVs. The other difficulty with finding spares is that parts for these big-box specials are not
readily available to the public. The boards have identification numbers on them, so that is where I started, with
internet searches.
AliExpress had some similar boards listed, but I found
more information on forums and in the comments on YouTube videos. It seems these same boards are used in several other brands. Searching for those gave me a lot more
information and leads on a spare from eBay.
I bought a whole new control board, and after a few
weeks, it duly arrived. It certainly looked the same; while
the revision number was slightly different, I threw caution to the wind, installed it and pressed the button. This
time, after a few flickers, the screen came up with a settings menu. I then went through it with the remote and set
it up as best I could.
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I don’t have an aerial lead out in my workshop, so it was
just internal stuff. I connected it up to the internet, and it
worked fine, loading the YouTube app and other free ones.
I assumed it would load their Netflix and Prime accounts
once they re-entered their details and registered the new
hardware ID. It was simply then a matter of buttoning it
all back up.
One job out of the way, then, but it would still very much
be in the way in my small workshop until they picked it up!
Enter contestant #2
The second TV was slightly smaller, like a rumpus room
set that had been demoted from the main lounge for use
with the games consoles because the owners bought a new,
bigger and shinier one for the lounge. It was older, clunkier and just as dead as the first one.
This one was altogether more solid and harder to get apart,
with a few hidden – or at least obfuscated – screws. Plus
one safety screw, just to make life that little bit more difficult for me. Fortunately, I had a long screwdriver that could
reach down the deep plastic tunnel and access the screw.
What really rots my togs is that some designer at the
company sat in a meeting with the brass and put this idea
forward, and it was accepted. They must know it won’t
stop people opening the thing up, but they do it anyway,
no doubt incurring more expense as yet another step in
the assembly process.
I eventually managed to get the back off the set, breaking
several of the now brittle-from-heat clips that also held the
shell together. Once the back was off, which also included
undoing the VESA mounted bracket, I could see the three
boards inside.
This TV is a house-brand device from another big-box
store here. This time, there were no identifying part numbers on the boards, and some of the IC’s had scraped off
numbers (thanks!).
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I suppose that someone used to repairing these or dealing with them would know where to source parts, but even
after I took pictures and tried several search-engine image
searches and Chinese site searches, I could not find anything even remotely similar. My usual forums were also of
no use; nobody seemed to know who made these things.
I’d taken it as far as I could, so I called the client and
said sorry that I was unable to do anything with it. Perhaps they could go back through the vendor and hope for
a repair there? I heard weeks later that they did just that
and were told it was obsolete and non-repairable, which is
increasingly the mantra for electronics and appliance vendors these days. The amount of e-waste this terrible policy
creates... Don’t get me started on that again!
The next job on the list was a turntable, a now-vintage
Sansui that back in the day would have cost the owner
a pretty penny. This one had been sitting in a container
beside the sea for over 20 years, unused, and the other
components in the stereo system fared about as
well as the turntable did.
The speaker cones were rotten through, the
metal baskets supporting what was left of them
corroded beyond repair. Lord knows what
the insides looked like; I envisaged the
crossovers looking like something you’d
recover from a shipwreck! The amp
looked as if it had its own ecosystem growing on it and the tuner
looked about as dire as the amp.
All this gear was top-of-theline back in the 1980s, but now
it looked as if it had been at the
bottom of the sea. I flatly told
the guy I couldn’t take that
kind of restoration on.
Not only would i t c o s t
a fortune to
replace all the
rotted parts,
there would be
no guarantee it
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would even be as good as it once was. That’s assuming
we managed to find new-old stock parts (he wanted to
keep it vintage) and could actually get it working. I just
wasn’t prepared to embark upon that sort of quest.
He asked if I could look at the turntable at least,
and I reluctantly agreed to check it over. He said
it worked but made a grinding noise while running. Oh, great. I could just imagine what the
bushings and all the motor bearings were
going to be like inside, not to mention the
state of PCBs or belts (if any) that might
be in there.
The only thing I could do was to remove
the Plexiglas lid and open the thing up to have
a look. The platen wouldn’t just lift out, like
many I’ve repaired, so it was likely held with a
clip underneath.
Like most devices of this era, chunky screws
held everything together and it’s just a matter of
elbow grease to remove them all. Most came out
cleanly, but a few were stubborn and needed a little help
to let go. Corrosion really does get everywhere.
Once the timber base was off (which could actually be
easily restored, even though it is only veneered Weet-Bix
wood), it was evident this was a project too far, for me at
least. The inside reflected the outside. Everything had a
powdered layer of corrosion.
It would require complete – and I mean complete – disassembly, cleaning and restoration, and reassembly before
it would work again. I am not set up for this sort of work,
and even if I was, I doubt I would take on such a time-
consuming task these days.
I am sure if this customer set up an alert on the local
auction sites he could pick up a good one for a fraction of
the price I would have to charge to repair this one. This is
where repairs truly make no sense. Unless someone has
a deep sentimental attachment to any given appliance,
there is a point where we just have to say, that’s it,
and pull the pin.
Even though this thing was in storage for
20 years, the owner kept hassling me to
get it done for some party he was having
in a week. He wanted to play records on
it, which had been in the same storage container. As if this would ever be a seven-day
repair anyway! Oh well, such is the life
of a serviceman.
Australia's electronics magazine
The last job
My last related job is
a DVD player a client brought in. The
whole DVD thing is
a bit like watching
the slow but sure
decline of vinyl and
CDs all over
again. The
problem is, of
course, that
most of us still
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have shelves packed with CDs and DVDs. Letting all that
go is just as bad as those people who have thousands of
records in their collections and can’t let them go either.
Keeping the machines that play these media alive is a big
job now because, aside from ultra-high-end players or bigbox store cheapies, there’s not a lot in between to choose
from. At least, not here in New Zealand.
So, the customer brought in a brand-name player to
see if I could get it going. It powers up but cannot detect
a disc in the player. I’ve seen this before in many a computer CD-ROM or DVD-ROM. It is usually because the laser
has simply gotten tired from use and cannot focus on the
disc sector that tells the player it is loaded, so it just keeps
hunting for one.
Many people say their drive doesn’t get much use. However, every time you access This PC or My Computer, or
turn a DVD player on, the laser fires to see if there’s a disc
in there. So it does some work even when not needed, even
if there is no disc present. Over time, the laser just wears
out, for lack of a better or more technical term.
I have done laser diode swaps in the past in expensive
units, but they are an absolute pain to get out of the heatsink/caddy the diode is pressed into. That’s once you drill
down to that level to get to it, which in a DVD player is
a mission in itself. So I wasn’t about to consider doing
anything like that with this one, if that’s indeed what the
problem was.
The rub is there’s no way of knowing until you swap it
out and try it. Once again, I had to do a hard pass on this
one. Good quality Blu-ray and DVD home-theatre type players are out there, and often not expensive, so I suggested
the customer looked into something like that.
The reality is that with high-definition streaming and
relatively inexpensive services, physical media is quickly
becoming superseded. In our household, I cannot recall
the last time I used my DVD player. Perhaps I’ll gift it to
this guy to replace his dead one.
Editor’s note: many people are going back to physical
media due to the fragmentation of streaming services and
the ongoing cost of subscribing. Many classic TV shows and
movies are no longer available, some even being removed
after people had “bought” them! Others have been doctored or censored. So don’t throw away those CDs, DVDs
and Blu-rays just yet! For example, see siliconchip.au/
link/ac1k
Saving two broken laptops
I wanted to send my mate a laptop, so I looked through
some I’d had for some time. I decided to repair an Intel Core
i5 based laptop we’d previously given to a friend, which
had come back broken. The bottom shell was badly damaged, but the rest was in good condition.
I was able to salvage an almost identical shell from a
similar laptop with lower specifications. The only difference was that this older laptop didn’t have an HDMI port,
so I had to cut a hole where the HDMI port was located on
the original motherboard. This repair went well and the
laptop was shipped off.
I also noticed an Acer Aspire laptop among the ‘junk’ that
looked like an easy repair. It was missing the keyboard, but
otherwise, it was in good order and also had an i5 processor. It wasn’t high-tech any more, but it was good enough
for web browsing and emailing.
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November 2024 99
I fitted some RAM, plugged in a USB keyboard and a
charger and pressed the power button. An initial test confirmed that it worked, so I fitted a 500GB hard drive, but
something was wrong. The hard drive went in way too easily. I removed it, looked closer, and found that the SATA
port was broken, basically writing off the laptop.
How could this laptop be salvaged? I had a thought. I got
a 32GB microSD card, put it in an adaptor, and inserted
that into the SD card slot. I booted the laptop from a Linux
disc and installed Linux on the SD card. I rebooted the
computer and it was up and running.
The entire installation used only 9GB, so there was plenty
of room left to install other programs. That was an easy way
to fix and give this broken laptop a new life. Still, I wondered if I could replace the broken SATA hard drive socket
so I could fit a 500GB hard drive to install Windows 10 on.
I’ve junked a lot of old laptops over time, most of which
no longer worked or were really old and in such poor condition that they were unrepairable. However, I’d kept the
motherboards, screens and other useful parts for future
repairs. I’ve previously been able to salvage USB ports and
mouse micro-switches for other repairs, but could I replace
a serial ATA socket?
I looked through the old motherboards and was surprised
at the variety of different SATA sockets. I only managed
to find two that looked like they were the same as the one
I wanted to replace. After dismantling the laptop, I found
that only one was precisely the same, the other one being
slightly different, as it sat closer to the motherboard, so it
was unsuitable.
I considered how to remove the SATA socket from the
scrap motherboard. I could either use my heat gun or my
80W soldering iron. I decided to try the heat gun on the
socket I didn’t need as a test. While I was able to remove
the socket in one piece, it did suffer some slight damage;
not bad enough to make it unusable. Still, I decided to use
the 80W soldering iron on the socket I needed instead.
I successfully removed the socket without damaging it,
so it was time to desolder the socket from the good motherboard. I got the socket off successfully with the same iron,
but it was quite tricky to remove, as it broke into many
small pieces in the process.
Now I had to work out how to clean out the tiny holes.
I got my desoldering iron, which uses suction to remove
the solder. This process was very tedious, but with
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perseverance, I got all the holes cleaned out. I fitted the
new socket and soldered it in place with my 20W soldering iron. It was time to reassemble the laptop and check if
the repair was successful.
With the laptop reassembled, I fitted a 500GB hard drive,
connected the charger and USB keyboard and pressed
the power button. I then pressed the F2 key and waited
for the BIOS screen to load. The repair was successful,
as the BIOS screen showed that the laptop detected the
hard drive.
I was unsure if this repair would be successful, with
the delicate nature of removing the SATA sockets and fitting the new socket to the motherboard. It seems that I had
good luck this time.
Now that I knew this repair was successful, it was time
to install Windows 10. I used the Windows 7 product key
on the back of the laptop, as I had done many times before,
but it said I did not have a valid key. What was going on?
I looked online and found that Microsoft had just closed
this upgrade path. I found a website selling genuine Windows keys at a reasonable price, so I paid for one and it
worked. Now the laptop was all good again, so I ordered a
new keyboard and fitted it. The repair was complete, and
the laptop was saved.
B. P., Dundathu, Qld.
An impediment to learning
Recently, I was behind a car in traffic and noticed that
every time the driver applied the brake, one tail light went
out. I have some experience with this simple fault, but it
can cause frustration for those who happen upon it for
the first time.
Back in the 1960s, I did my time as an electrical apprentice with what was then the South Australian Railways,
mainly at the Islington Railway Workshop.
During my training, I was exposed to repairing, maintaining or installing various equipment ranging from low voltage DC (automotive electrics), higher voltage DC (32V, 64V
and 110V on rail cars and locomotives), batteries, 240/415V
AC industrial machinery, power tools and domestic appliances as well as switchboards for equipment control circuits, lighting and air conditioning within carriages.
It was during my stint looking after the battery shop and
vehicle electrics that I encountered the brake/tail light fault
and learned an enduring lesson.
Several years later, I was working in an Army workshop
in Hobart as the resident electrician when one of the tradesmen from the vehicle service station begged my help with
a Land Rover that had a tail light problem. On arriving at
the service station, I was confronted with a vehicle with all
the covers off and switches and wiring exposed.
The mechanics had spent the best part of five hours trying
to find the source of the fault and were not amused when
I showed them a high-resistance chassis ground connection on the offending tail light. My input took about three
minutes, leaving them with several hours of work putting
everything else back together.
Back in my apprentice days, the standard multimeter
we used was the AVO 8, a reliable device but rather hard
to carry and use compared to modern meters. The AVO
was a relatively low-impedance meter compared to today’s
devices. Late one afternoon, a carriage traverser stopped
working, which was needed in service the next morning.
Australia's electronics magazine
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A carriage traverser is a section of rail on a platform
that can move sideways to transfer rolling stock from one
track to another parallel one. The traverser had a threephase motor to drive the axles to effect the track changes,
but there was no power to it. It came via an underground
mains feed to a pit, then up a pole via contactor to overhead catenary cables to pickups on the traverser.
Being the youngest, I was sent into the pit to test for
power to the catenary feed and had the AVO 8 in hand.
One of the engineers who had come to see what was happening had a brand-new high-impedance “Sanwa” meter
that had arrived only a day or so previous, and passed that
meter to me to use instead of the AVO.
Using the Sanwa to measure between phases, I got readings of 360V AC and 730V AC instead of the expected 415V
AC. That had us all scratching our heads. Swapping back
to the AVO, the readings were all zero; another puzzle.
Looking upwards, I noticed that the high-tension overhead power line ran parallel to the underground feed. I
then realised that the high-impedance meter was reading
an induced voltage from the overhead supply. A failed
supply fuse to the three-phase contactor was the cause of
the fault, and that was easily fixed.
Twenty years later, I was working as a supervisor in an
electrical workshop at Puckapunyal when a trainee attempting to diagnose a fault on a water cooler was confounded
when the wires to a small terminal strip, including switch
wires, were all showing 240V to Neutral. He was using the
standard issue Fluke multimeter.
Sensing déjà vu, I took the Fluke away, handed him the
Army “Aust Mk II” multimeter, a low impedance meter,
and asked him to repeat the measurements. It was his turn
to learn about induced voltages and high-impedance measuring devices. Some lessons learned early never fade.
G. D., Mill Park, Vic.
Hickok TV-7 valve tester repair
My TV-7 D/U valve tester failed the other day. The meter
was stuck and moving erratically and the “line set” could
not be completed at switch-on. I immediately thought that
the meter had failed (which it had), but the mode of failure
was what surprised me.
I have had this tester for about 12 years. I bought it on
eBay when I was living in Tokyo; it’s ex-USAF and has a
colourful history. It is in remarkable condition (my alltime favourite). At the time (2012), our dollar was close
to parity with the USD, so this tester ended up costing
me about $450.
I bought about 20 pieces of equipment and had them
shipped straight to Australia before the “Harvey Norman”
tax on imports; times were good!
Anyway, I pulled the meter and removed the Perspex
lens, and then suddenly the meter worked perfectly again. I
figured I’d put it back in and try it out. I got the same problem; in fact, just wiping my finger across the front caused
the meter to move and get stuck in weird positions.
These meters were made by Phaostron. They are great
because there is a knurled knob inside that you can adjust
to change the full-scale deflection (FSD). It works as a
magnetic shunt, allowing more or less magnetic intensity
through the moving coil (even HP didn’t have this).
However, apart from this chestnut, the meters are jewel-
pivot, not taut-band like HP. Still, I have never had a single
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November 2024 101
one get stuck, and I have played with hundreds (another
story)...
The problem was that the plastic lens on the front was
retaining a static charge, causing the needle to misbehave.
Most Phaostron meters had an anti-static coating on the
inside of the Perspex to prevent that, but perhaps the coating has broken down over the last half-century.
I was very surprised as this meter never had any static
issues like you expect to see in cheaper plastic meters.
Again, this is where the big old HP meters triumph, as they
were constructed with anti-static Bakelite and glass lenses.
The resolution was to pull the guts out of the meter and
transplant them into another Phaostron housing that was
made much later (circa 1980s). This had a glass lens; obviously they realised the problem with plastic, or ruggedness
was no longer a USAF requirement. In any case, the meter
now works perfectly again. Happy days!
D. V., Hervey Bay, Qld.
Seiko wall clock repair
I am sending this in case someone has the same trouble. I probably would not have bothered to fix it because
I have too many clocks around the place as it is, but this
one has been with me for around 50 years and has a lot of
sentimental value.
The clock used to keep good time, but over the last
couple of years, it was out by up to 20 minutes a month.
Try as I may to adjust it, I always failed to get any sort
of accuracy.
At the beginning of this year, it kept stopping but always
started OK. I overhauled the mechanism, which seemed
to fix it, but only for a while. Eventually, it stopped and
would not start, so I opened it up again and tested some of
the components. All tested good except for what I would
call the driver coil. I could never get the same resistance
reading twice. It varied from 3kW to 3.5kW.
The driver transistor was a germanium PNP type. It
was easy to remove, so I took it out and tested it, and
it was good. To see if a silicon transistor would work, I
replaced it with one of those with the closest characteristics. I set the clock up on the bench and it started, but
it only ran for a couple of days before stopping, and it
would not start again.
That meant the driver coil was faulty; I suspect it had
intermittently shorted turns. I removed the tape from the
coil and found that all the connections were good. I then
put the coil on a spindle and unwound all the wire; there
were no breaks. I tried to rewind it with some wire off
another coil but did not have any success.
If the bobbin hadn’t had mounting feet on it, I may have
got away with it. But my 77-year-old eyes were watering
just trying to see the 0.076mm diameter wire, and when
it broke, I gave up.
I looked in my relay box but could not find a coil with
a big enough hole up the centre for the pendulum rod, so
I left it on the bench in case an idea came to mind. I later
had a thought that a washing machine water solenoid coil
might do the job. I had some in a box and found a few that
measured 3.6kW, so I removed the coil.
The centre hole was smaller than the original in the clock
but large enough to fit over the pendulum rod. By drilling
a 29mm hole in a piece of timber 20mm thick, cutting it
in half and drilling some holes for mounting bolts, I could
set it up to see if the clock worked. It did not.
The pendulum in this clock actually drives the gears
via a ratchet and pawl system, and the coil did not have
enough pull. I shorted out the 1kW series resistor, and
although there was an improvement, the clock still did
not run.
I had been wanting to run the clock from a rechargeable
battery in a holder at the bottom of the case to save me
having to take the clock down from the wall every time
it needed a battery change, so I tried two Eneloop NiMH
batteries in series, taking the voltage from 1.5V to 2.4V.
The modified clock runs fine with this arrangement,
even with the 1kW resistor back in the circuit, and has been
doing so for four months. Not only that, but once I got it
adjusted, it kept perfect time.
I slotted the holes for the coil mount and made a brass
plate with tapped holes for the screws. Now I can adjust
the position of the coil to suit where the pendulum rod
ends up, after changing its length to make it keep the correct time, without having to take it down from the wall.
I painted the coil and wood clamp black so they were not
visible with the glass door closed. I left the original transistor and coil former in the bottom of the case.
The curved rod that enters the coils has a magnet on
both ends. It induces a current in the coil large enough to
switch on the transistor at the right time.
SC
R. G., Cooloola Cove, Qld.
The internals of the Seiko clock, showing the curved rod and coils (left), and the modified circuit diagram (right).
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